Sign my

LTM 51


Making the pivots became an adventure and a small project in itself so I dedicated this separate page to the subject of making the pivots.

The pivots are the central connection between the boiler cradle and the two power units.

The etch set and its documentation give no clue whatsoever how the boiler cradle connects to the power units. Garratts had pivots so I wanted to mimic them. The pivots had to meet quite a list of demands:

  • The pivots should allow free movement in the horizontal plane.
  • They should also allow some movement in the other two directions to allow for uneven track conditions.
  • There should be no significant side play, the pivots should prevent the boiler cradle to go visibly off center, 0,1 mm in either direction would be about the maximum.
  • The pivots should also provide stability to the boiler cradle so that the latter will not wobble during running other than caused by the track condition.
  • The pivots may not protrude above the boiler cradle's running board in the form of a bolt as it would be very visible there.
  • Likewise the pivots may not protrude below the power unit's running board as this will probably interfere with the gearbox.
  • It should be possible to disassemble the pivot for maintenance purposes.
  • The pivot should be sturdy enough to lift the loco by the boiler cradle without the risk of the power units falling off or otherwise damaging the loco.
  • The height of the pivot is limited to 5.5 mm between the bottom side of the boiler cradle and the topside of the power units.
  • The pivot may not protrude from under the boiler cradle's front and rear end. Total invisibility is not required as long as it is not too obtrusive.
  • And finally the pivot's design should be such that I can make it myself. I can think of a zillion better designs than I finally realised but there are only a few that meet all criteria and are doable as well.


You may notice I did not mention anything in terms of piping, power drives or wiring going through the pivots. Correct.

  • The piping on a model is non-functional anyway so I will mimic it as faar as possible but it will not go through the pivot.
  • I decided to power the drive units individually instead of using a central motor with universals
  • Electrical wiring would have been nice if it could fit through the pivots invisibly but for one it would show up on the top side of the running board and it would make matters unnecessarily complicated.

So the pivots have the sole function of making a moveable connection and nothing else.

Two shots of my own of the real thing: an NGG16 pivot on the front of the boiler cradle and its counterpart in the bogie.
Dinas, Wales, 2017.


With this list in mind I thought out numerous contraptions, with and without springs, with and without bolts.

After a week or so I came to this design for the cup and that kept coming back. The most important objection was its feasibility: can I make this? The top part already had the mushroom-like shape in my mind. But the under-cup was just too difficult to make.
After many iterations I came to this simple design. A cup with a bottom and a mushroom top part. The recess in the mushroom was there to take up two bolts that would prevent the pivot from falling apart.

New in the workshop


A few days before work really started this Quick Change Tool Post for my Unimat 4 arrived.

A QCTP allows you, as you can suspect, to quickly remove and install tools. But the individual toolholders also allow you to adjust the height of the tool which is a considerable bonus. Having this QCTP really saved me a lot of non-productive time during the making of the pivots. It already paid itself back!


I bought the QCTP from Chronos Engineering Supplies. I used their Special Offer which comprised the standard QCTP and two tool holder (currently at £35.94) and which also included another six additional tool holders (currently £8.87 each), on offer for just £58.80 incl VAT (so saving me about £30 on the total of £89.16). The toolpost itself is well made. The

individual toolholders are a bit crude but they do the job well. Order went quick and delivery time was good considering the corona crisis and the consequent delays in mail orders.


A QCTP from almost identical design is available from Emco Machine Tools, but then costing a staggering £72.00 for the post plus two tool holders and separate tool holders for £22.80 each which totals £208.80. As far I can judge they are not really different from the ones I bought, but maybe they are finished a little less coarse. It is not possible to judge that from the photo.


Thee Emco Shop in Austria seems to go completely wild. They sell original Emco QCTP's of very much the same design costing a fat €116.40 (£104.03 as per 25 May 2020) and separate tool holders will put you back €37.20 (£33.25) each, totalling €339.60 or £303.53. As I cannot get a decent picture of them I can not judge if the quality is so much better than my el cheapo.

So to recap

  QCTP + 2 holders extra holders (each) Total QCTP + 8 holders
Chronos Engineering Supplies £35.94 £8.87 £58.80 (offer)
Emco Machine Tools £72.00 £22.80 £208.80
Emco Shop in Austria £104.03 £33.25 £303.53


Actual work


I started with drilling a 6 mm hole in a piece of 12 mm brass stock. From there I wanted to enlarge it to 8,5 mm and at the same time flatten the bottom of the cup to the desired depth, keeping about 0.5 mm braas as bottom.

The one big problem I encountered is that all the tools I have are simply too big for the job. A 6 mm carbide cutting tool is by all definitions in the engineering world small, yet way too big to get in this cup.

After considerable effort to get the job done with the tools available I ground a broken centre drill to the form of a tool and went with that. It did not seem too big but once again I had to squeeze it into the cup. I just could not get it right. So when I was done, the outside was good, but the inside was a mess.

Then I found a very small centre drill in my forgotten-small-and-suitable-centre-drills box, only 3 mm in diameter and managed to grind it into a reasonable tool. Next problem was how to hold this tool. I took a piece of 6 mm brass rod and drilled a 3 mm hole. On my Proxxon drill stand I sawed a slit with a cutting disk. When the holder is clamped this slit is compressed and clamps the tool.
Now I could decently get in the cup and wow! The chips came flying out. I ground the tool so that I could get in in the X-direction and then sheer out in the Y-direction widening and than deepening the hole in one stroke. On the fly I learned to gauge the depth of the cut.

This gave a far better result on teh second attempt. Some chatter is visible in the surface but hey I am a beginner!



Before long I had a second cup and one mushroom that went well together.

The first mushroom went so well I forgot to take photos. Total height of the assembled pivot: 5.4 mm, just 0.1 mm short of the spec. There is a little more side play than intended but not conspicuously so, 0.2 mm to either side. I even managed to remount the very scored first attempt and clean up the inside of the cup from all its scoring and marks. So now I had two suitable cups and one mushroom. Three down, one to go

Maybe I became overconfident, the second mushroom snagged the tool while cutting the recess and it whizzed through the workshop like a bullet. The damage to the part bears witness to its violent escape. Luckily no harm was done other than to my self-esteem. And that can do with a dent. I was clearly warned though, this may be modelling, it still has risks.
Once the second mushroom had been completed I drilled two 0.8 mm holes in each cup.

and tapped the holes M 1.0

Tapping was done in the Proxxon drill stand. It is extremely difficult to tap such small sizes. Breaking a tap would be disastrous so I took no risk. Please be aware I did not use the drill as a motor tool. With 5,000 rpm it would have spelled disaster. I used it solely as a guiding mechanism to get the tap in straight and keep it straight during tapping. I turned the head by hand, feeding the tap with the drill stand's handle with the feel that this gave.

Two M 1.0 bolts were cut to suitable length.

The pin, 0.7 mm, demonstrates that the top can tilt a little but this tilt is restricted by the bolts.

Two done. Holding it in the palm of my hand makes it tangible how small these part are.

Test and verification

I cut the form of the power units and the boiler cradle from 0.5 mm styrene to see how things would work out. I glued the pivot parts with simple household glue.

One of the things I wanted to know was if I could still get to the bolt heads to assemble and disassemble the pivots.
Although the pivots will protrude through the front stretcher of the boiler cradle's frame I hope it will not be too conspicuous once painted black. Modelling is compromising and here is my compromise: the function of the pivots is more important then scale correctness.

The boiler was glued on as a weight to see if the boiler cradle was stable enough on its pivots.

I also tested if there was enough play in the vertical planes to let the model cope with uneven track. Well, I think this is more than enough.


The photo left nicely shows how the top part lifts from the bottom part.


Conclusion: the pivots are fit for the job! Mission accomplished.

Now it is time to continu with the construction of the boiler cradle.